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Beolover SyncDrive: DC Platter Motor Replacement for Beogram 4002 and 4004 (Type 551x and 552x)

Late Beogram 4002 and the 4004 (Types 551x and 552x), which have DC platter motors instead of the earlier synchronous AC motors usually suff...

Showing posts with label 2120MFBG8002. Show all posts
Showing posts with label 2120MFBG8002. Show all posts

Sunday, May 4, 2025

Beogram 8002: Re-Assembly and a Joyful Test Spin with Manfredo Fest

I recently performed a functional restoration of a Beogram 8002 that I had received from a customer in California. This Beogram was in pretty decent cosmetic condition overall, but had a fairly scratched hood. Luckily, the dksoundparts store has new reproduction hoods that look very identical to the original ones. The only issue is that the original aluminum hood trim needs to be transferred if one wants to retain the original B&O labeling. Dksoundparts only offers a generic trim strip for fear of lawyer letters from B&O's suit wearing set. Luckily Co-Beolover Beomazed figured out how to remove the original trim from an original hood without damaging it! 

So, while I was playing the restored Beogram in 'service position' to see if it had any intermittent issues left to cure, I sent the hood to Beomazed and he transferred the trim. This post discusses how he did it. It is a pretty challenging and tedious procedure (and of course involving the heavy use of a Dremel tool!!...;-).

He did an awesome job! The trim did not suffer at all and the new hood looks absolutely pristine!

So when I received it back I re-assembled the deck with the new hood. Here are a few impressions:



Very beautiful! Time for a test spin with Manfredo Fest! I recently discovered this interesting Brazilian keyboarder and composer. It is difficult to find his original vinyls, so I bought a re-issue of his possibly most known record, "Brazilian Dorian Dreams" which was initially released in 1976 on T&M Productions. The re-issue is from the British label Far Out Recordings (FARO219LP). It sounds pretty god in my opinion and the pressing is of high quality with only few clicks and pops. It is available via Amazon in the US. The title song Brazilian Dorian Dreams was an equally educational and joyful experience to me. It is written in the Dorian scale, which I had never experienced before, I think. It gives the track a remarkable sound, which I seem to enjoy very much. The wonderful voice of the vocalist Roberta Davis is probably not hurting this experience either! Check it out, it is definitely worth it! The album is on Spotify for a quick discovery.
Here are a few shots of this magnificent record playing on this fully restored Beogram 8002:

Very Beolovely! I will now play a few more records and then it should be time to return this nice Beogram 8002 to its owner!



Sunday, April 13, 2025

Beogram 8002 Hood Replacement

 The Beolover recently received a Beogram 8002 from a customer in California. As part of the restoration, the customer elected to have the hood replaced with a new one. Luckily, these hoods are now available from the Beoparts store.

The main issue with the reproduction hoods is that you don't get the original trim strip that has the model designation. Beoparts does offer a replacement trim, but it's not an exact match for the original (the original varied over time also, some are brown, some are black), so the best solution is to try to preserve the original.

This is the condition of the original hood, it shows the typical wear and tear:


A lot of that damage could be avoided in the future by using softer cleaning solutions such as a damp microfiber cloth. Windex and paper towels are abrasive to plexiglass.

Believe it or not, the photo below depicts the first step in the process I use to extract the original trim. It took several attempts to get this process perfected, I wouldn't recommend it unless you have spare hoods!



The reason for cutting the hood like this is that it's too difficult to work with the large hood and its structural rigidity causes more stress on the trim piece. When cut down to this size, the hood is more flexible and can flex away from the trim, without bending the trim. I apply heat for an extended period of time to loosen the glue and I am then able to pull them apart:


The back side has a layer of glue which must be removed, the X-acto #17 is perfect for this:

Back is pristine, ready to be glued down to the new hood:

The front looks great, has a minor scratch:


I then use masking tape and paper to protect the surfaces while spraying high bonding strength adhesive on the back side of the trim and top of the new hood:


Here's a peek at the final product, which the Beolover will be completing very soon:





Saturday, April 5, 2025

Beogram 8002: Full functional Restoration and a Test Spin with Cannonball Adderley

This post discusses the functional restoration of the Beogram 8002 that I received from a customer in California a while ago. This post discusses my initial assessment of the unit.

When I work on a Beogram 8002 or 8000 I usually extract the technical parts from the enclosure:

This makes it much easier to work on them. This unit had some mechanical issues with the carriage. The first step is always to extract the parts that guide and move the carriage for cleaning:
A 30 min run in my ultrasonic removed the original lubricants and the parts could be reinstalled. At this point I also adjusted the tone arm parallelism since it is necessary to have the carriage up for the vertical adjustment.
Next I focused on rebuilding the PCB. Often the electrolytic capacitors are out of spec or even short circuited. Another common issue are bad solder joints on the board headers. This shows the board in its original condition:
I removed the microprocessor can and replaced all the capacitors:
I also added small 'hooks' to pins 4 and 6 of P5:
They are useful for connecting a multimeter for doing the <</>> button adjustments later on.
The perhaps trickiest part of the board restoration is replacing the decoupling capacitor (C28) that stabilizes the power supply of the microcontroller. Such capacitors need to be placed close to the to be decoupled device and therefore it is located inside the can:
I opened it:
The capacitor is found after lifting up the small additional board that is inside:
This shows the solder points from the bottom:
The tricky part is that the ground lead of this capacitor is also used as a ground via, i.e. is soldered to pads on both sides of the board. 1980s technology is fun!...;-). Since there is not much space around this capacitor it needs to be destroyed for removal. I usually unsolder the 5V lead first and then pull it upright. The next step is rotating the capacitor until the ground lead breaks and it can be removed:
With a desolder pump the remaining fragment of the lead can be extracted and the pad cleaned on both sides. Installation is reverse. With a small tip solder in the ground lead on the component side and then on the solder side, followed by soldering the 5V lead:
After this operation I closed the can back up and re-installed it on the baord:
Then I reflowed all the board headers. Especially the one that connects to the transformer block is often affected by broken out solder joints, which causes intermittent power to the deck. I usually ad a bit of solder to those points to make them stronger.
The next step was replacing the output relay, which is often oxidized. It is mounted under a shield inside the DIN7 output connector assembly: 
The shield is just clamped to the relay and can be pulled up easily:
I replaced the relay with a new Omron relay with the same pinout:
Nowadays such relays are fully enclosed, which should make them last longer. The relay I used has the same lateral dimensions like the original relay, which makes it easy to put the shield back on:
In many cases there is a hum when connecting the 8002, espeically to RCA type inputs. This hum can be quenched in most cases by connecting system and signal grounds. I usually install a switch on the output assembly that allows choosing whether to connect the grounds or not. It is convenient to solder it directly to one of the big GND pads on the PCB and make the signal ground connection with a wire:
There are two more capacitors (OC1/2) that need replacement. They are directly soldered to the voltage regulators that use the floating chassis as heat sink:
This shows the new caps in place:
One more in the transformer block:
This capacitor is responsible for the phase shift necessary for the second motor phase. Since the motor runs on AC this one is a non-polar electrolytic capacitor. It can be replaced with two back to back polar units, like I did it in earlier days, or with the more modern Beolover Motor Capacitor for Beogram 8000 and 8002, which is designed based on modern SMD ceramic capacitors. Those do not care about polarity and so are the perfect choice for this application. The board is set up that it can be used in both 50 and 60 Hz configured Beogram 8000 and 8002, which need different capacitances for the proper phase shift. In this case the unit is a US 110V/60Hz unit and so I used the smaller 27u capacitance:
After closing up the transformer box I focused on replacing the light bulb that enables the pressure sensitive gradually adjustable << and >> carriage speeds with an LED. LEDs emit light in a more consistent way over time, which is important in this case since the light intensity permitted onto the photo resistors mounted on the sides of this assembly governs the carriage speed. The bulb is inside the black box on the board:
This shows the board from the bottom. From this perspective one can see the seesaw metal aperture component that is pushed down on either side with the <</>> buttons to change the amount of light on the photo resistors:
Removal of the top cover of the box reveals the light bulb and the two photo resistors:
I usually replace the bulb with a 5mm white LED that I sand a bit to diffuse its light emission:
Since LEDs run at a lower voltage than the bulb it needs a current limiting resistor, which can be conveniently added on the bottom of the assembly:
Then I plugged everything back together and adjusted the <</>> voltages by using the two hooks I soldered to P5 when I rebuilt the main PCB:
The two screws on the <</>> assembly need to be turned in or out until 620mV are achieved on the respective P5 pins.
After adjusting the tracking feedback to yield carriage movement after about 2 turns of the platter it was time to play a first record. I selected one of my all time favorites, "Somethin' Else" recorded by Cannonball Adderley together with an illustrious group of contemporaries including Miles Davis, Hank Jones, Sam Jones and Art Blakey in 1958. I currently only have the Blue Note 75th Anniversary Reissue (2014), which was (sadly) cut from digital hi-res transfers of the original analog tapes. Still sounds pretty good on this Beogram 8002 in 'service position'..;-):

The scratched hood is on its way to Beomazed, who figured out a way to transfer the original 8002 trim to new hoods from dksoundparts. Stay tuned!


Friday, March 28, 2025

Beogram 8002: A New Arrival from California - First Look

I recently received a Beogram 8002 for a full restoration from a customer in California. It was shipped in a Beolover double box shipping container and it arrived without shipping damages. This shows the unit after I extracted it from the box:

A few parts were packaged separately, indicating previous repair attempts.
The hood is fairly scratched:
The platter, aluminum panels and veneer panels are in pretty decent condition:
I opened the unit up:
The 8002 flips open like a book. It is a good idea to flip the top against a vertical support. I extracted the vital parts and put them on my bench:
After reconnecting everything I plugged the transformer in and the LED dot came on in the display. I pressed PLAY and the carriage went to search for a record. STOP returned the carriage home.
All good signs! Stay tuned for the restoration report.