This shows a detail photo of the replaced output relay and rebuilt delay circuit:
The added small red switch in front of the socket for the output cable allows connecting the signal and system grounds. This can be helpful if there is a humming issue when connecting the Beogram to a receiver.
I moved on to replace the 4th and final incandescent light bulb in this Beogram. It was located in the sensor arm and is crucial for the record detection system. This shows the small back compartment from the front of the sensor arm pulled out:
It is possible to bend the sides back straight with carpenter’s clamps and pieces of wood:
After 2-3 days, the bends are usually straightened out. It is important to get the frame sides as straight as possible, since otherwise it can be difficult to seat the aluminum panels properly on the Beogram.
If you try this at home, do not overtighten the clamps, or the wood may break.
At this point, the enclosure was empty save for the many transport lock bushing fragments strewn around:
I vacuumed the enclosure clean and wiped it down with a wet paper towel.
Time to put things back together! I started with the floating chassis. This shows one of the new transport lock bushings with its lock screw in the center:
Since this Beogram only used a single capacitance reservoir capacitor, all I had to do was tack on the white and black wires from the power plug of the main PCB.
I put the remaining components back in and fired the deck up to adjust the bias of 1TR3 (the sensor arm transistor) to get 4V at its collector. This needs to be done while the board is installed. So I solder the trimmer first to the solder side that I can access it for adjustment when the deck is powered up.
After adjusting the trimmer, I moved it over to the component side. Then it was time to check if the record sensor worked properly. I connected my oscilloscope between the collector of 1TR3 and ground and installed the platter. This is the trace I measured while spinning the platter with a finger with the sensor arm positioned over the platter:
Each of the dips represents a platter rib passing under the sensor. I measured an amplitude of about 6.5V, which is a nice, stable sensor signal.
My next task was doing the arm adjustments: First came parallelism. Both the sensor arm base and the sensor arm need to be perpendicular to the carriage rods, and the tone arm needs to be parallel to the sensor arm with a spacing of about 7mm. To get this often tedious adjustment right, I now use my recently developed
Beolover Arm Alignment Tool for Beogram 4000, 4002 and 4004:
I installed the wood plinth that by now had fairly straight side pieces, and then I started the process of aligning arms, platter, and floating chassis to get the platter parallel to the arms across their travel, and the platter flush with the surrounding aluminum panels. This can be an iterative process that takes a few passes to yield proper alignment.
Once everything was perfectly aligned, I replaced the flimsy circlip that holds the counterweight screw in place
with a M3 square nut and a washer:
This allows me to lock my calibration in place so it survives shipping the Beogram. Then I adjusted the arm-lowering limit:
This important adjustment helps prevent needle damage if the arm should ever be lowered onto an empty spinning platter due to a malfunction of the record detection circuit.
Next came the calibration of the tracking force. I usually adjust the counterweight so that the little scale on the adjustment wheel is accurate around the standard 1.2g tracking force that most B&O cartridges prefer.
In general, I recommend checking the tracking force once in a while with a small digital gauge like the one I use in the above picture. The adjustment wheel on the arm assembly is notorious for not being all that precise.
After these adjustments I installed my
BeoloverRPM device to characterize the performance of the DC platter motor:
The BeoloverRPM has two operational modes. In 'slow' mode (shown above), it measures the RPM in 10-second intervals and sends the data to a serial port of a computer, where it can be recorded with any generic terminal software. This allows plotting the RPM over long periods of time using Excel or similar software. This shows the result of my 24 hrs measurement:
This is quite a nice result for any Beogram DC platter motor! As good as it gets! The curve looks pretty much the same as
what I measured in 2020 when I originally restored this motor! This suggests that my oil-infusion process is long-term stable!
Next, I collected some high-resolution data in the 'fast' mode of the BeoloverRPM:
In this mode, the device sends an RPM measurement every time a platter rib passes through underneath the sensor. This gives 24 RPM measurements per platter turn (there are 24 ribs). This allows visualizing short-term RPM changes caused by the feedback-based motor control circuitry. This graph contains the data covering ~35 platter turns (~70 sec):
The prominent zig-zag pattern is a measurement artifact that comes from the fact that the spacing of the platter ribs around the platter is slightly irregular due to manufacturing imperfections. This generates a repeating pattern for every platter turn (sort of a 'platter fingerprint'), which is superimposed on the real RPM changes that are introduced by the feedback system that keeps the motor RPM stable over time. This real RPM change is essentially the sine-wave-like pattern that modulates the zig-zag pattern. An evaluation of the wavy component yields a wow and flutter estimate of about 0.1%.
This is 2x of the 0.05% stated in the specs list in the service manual. This difference is most likely systematic due to the entirely different way wow and flutter were measured in the 1970s when these turntables were produced. I see it for all Beogram motors that I restore. Back then, the measurement was carried out with a test tone on a test record. In these measurements, deviations from the tone center were measured with an analog spectrum analyzer and then converted into a wow and flutter number. It should be pointed out that this discussion is pretty academic in the first place since humans typically start recognizing frequency fluctuations above the 0.7% threshold, i.e., the RPM fluctuations of this Beogram are well below this threshold, whether the number is 0.05% or 0.1%. This motor is definitely ready for duty!
After this measurements completed, I replaced the original oxidized DIN plug.
with a new all-metal type that has nice gold-plated contact terminals:
The on-board RIAA pre-amp allows directly plugging the Beogram into any modern high-level input on current B&O or Sonos speakers, etc., or into an amplifier without a phono input through a CD, DVD, or AUX input.
Since this is a 4004, the Commander gets its power from the output board. This requires the installation of the white 4-wire harness that connects the Commander board to the RIAA board. The Beolover RIAA already has the appropriate Commander jack broken out, so the normal Commander adapter for the keypad connector does not need to be used. I stuck it into the keypad jack of the original output PCB in case this Beogram will ever be used with the original output setup:
Next came the installation of the keypad. This was the moment for swapping out the smudgy original keypad with a newly rebuilt one. This shows old and new in direct comparison:
See
here if you are interested in fixing or getting your keypad fixed. A new keypad is a great way to significantly increase the cosmetic appeal of a Beogram!
The original keypad also had broken-out plastic fixtures that hold the RPM panel in place:
Luckily, there are faithful reproductions of these plastic parts available from the DKsoundpartsstore in Denmark:
All that needs to be done for implementing them is transferring the metal springs over from the original ones:
This shows a new one installed on the rebuilt keypad
Then it was time to plug the new keypad in. This shows how the grey keypad plug goes into the jack on the RIAA board:
The black main plug of the keypad goes into the jack on the Commander board. This shows everything in place:
And then it was finally time for a test spin with this beautifully restored Beogram 4004!
I selected one of my favorite Eddie Henderson records, "Mahal", which he released in 1978 on Capitol Records (
SW-11846). Herbie Hancock and Hubert Laws are among the players. A very interesting record in my opinion! Here is an impression of this lovely album playing on the restored Beogram!
Beautiful! I will now play this Beogram for a couple of weeks to see if there are any intermittent issues, etc.
The first step is removing the original hood from the metal hinge assembly. I detached the aluminum trim on both sides using a razor blade:
The hood can be removed after the two screws are removed on both sides.
It turns out that this hood was close to cracking off the hinge anyway. The typical stress fractures were already well-developed near the bolt holes:
The first step for installing a new hood is always checking if there is an interference between the plastic and the metal hinge bar. If the plastic chafes on the metal, it can cause the hood to crack off the hinges. Therefore, I bolt the hood to the hinge for a test before I go ahead with the installation, and then manually work the hinge while watching if there is any touching. The problem usually occurs close to the hinges as indicated below with the red frame:
This hood demonstrated a safe minimum distance of about 1 mm across its range of motion.
After this successful test, I went ahead and glued small 3D printed plastic bits into the strange 'channels' they designed into the sides of the hood where the aluminum trim goes:
After the epoxy hardened, I trimmed the plastic bit with a razor blade to smoothly continue the corner in the plexiglass:
The purpose of the plastic bits is to help make a sharp bend in the aluminum trim around the corner. The 'channel' causes a void at the edge under the aluminum, which makes it difficult to make a good bend.
Then it was time to center the new aluminum trim. I used my 3D printed alignment pieces and a stretch of blue tape
to make an alignment pencil mark:
Then I bolted the hinge assembly back into the hood. I usually put a bit of white wood glue on the threads so the screws stay put. One cannot tighten them very much. Too-tight screws can also cause a premature cracking of the hinge areas of the plexiglass.
The next step was attaching the
new aluminum trim and then making the bends down the sides using my bending block.
Beolovely!:
The final touch was installing the rubber bumpers into the holes on the front corners of the hood:
The provided bumpers have stems that are a bit too short in my opinion and they can fall out fairly easily. For this reason I usually put a bit of superglue gel into the holes before I put the bumpers in.
This completed my work on this Beogram 4004!
Here are a few nice pictures of this fully restored Beogram 4004. Enjoy!