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Beolover SyncDrive: DC Platter Motor Replacement for Beogram 4002 and 4004 (Type 551x and 552x)

Late Beogram 4002 and the 4004 (Types 551x and 552x), which have DC platter motors instead of the earlier synchronous AC motors usually suff...

Wednesday, April 8, 2026

Beogram 4002 (5503): Replacement of a Loudly Humming Transformer with a Modern Universal Power Supply

Oh well, after playing the lovely Beogram 4002 (Type 5503) that I recently restored I had to realize that the transformer made a pretty loud humming noise, which was quite noticeable during lower volume music passages. Especially, when placing the unit on a wooden sideboard the resonance of the wood amplified the hum to quite annoying levels.

I decided this definitely needed fixing before I could possibly sell this unit. A welcome project since I thought the initial crop of AC motor Beograms also needed a universal power supply upgrade similar to what I recently developed for the later DC motor models

Modern monolithic universal power supplies have several advantages over the original transformer/rectifier based setup: They are usually short circuit proof, they do not hum in any audible way and they mostly are designed to run on grid voltages ranging from 100V to 240V, i.e. can be plugged in anywhere on this planet. This feature also makes them brown-out resistant and they will also reliably protect the Beogram circuitry from voltage spikes etc...

The reason why my solution for the DC motor Beograms cannot be used in the AC motor models is these have a more than 3x higher power rating. DC motor Beograms are rated 15W, while the AC motor models are rated 50W. This difference is mainly caused by the AC platter motor, which is a power hog. This explains why the older Beograms get much warmer than the later ones.

It means that the 25W Meanwell supply I utilized for the DC motor Beograms is not powerful enough to run an AC motor model. Further investigation yielded that similar supplies rated for higher output had a too large footprint and would not fit into the space vacated by the transformer.

After a bit of poking around I found a more advanced design made by Traco that combined a small footprint with a 30W output: The TPP 30-D Series, which is a high-quality medical power supply. It is fully encapsulated and the output voltage can be adjusted (a rarity among this type of power block). The specific TPP 30-124-D (24V nominal) type can be adjusted to a maximum output of 26.4V by connecting an external resistor. This was great, but 30W is still not enough for the standard setup of an AC motor Beogram.

However, when combined with the Beolover Efficient 22.8V Power Supply and Main Capacitors for Beogram 4002 (Types 550x) 30W is enough. The Beolover 22.8V supply reduces the power consumption of the AC motor models significantly since it replaces the other power hog of this 1970s design, the linear voltage regulator, with a buck converter that has a high efficiency.

This shows the Transformer Replacement Kit for Beogram 4002 (Types 550x):

It includes the TPP30 supply mounted on the breakout board, the adapter necessary for bolting it to the enclosure bottom, the jumper for connecting it to the fuses assembly, the mounting bolts and a set of fresh fuses.

Let's see how I implanted the Traco TPP 30-124-D supply in this Beogram!

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Safety first: Potentially lethal voltages can be present during the installation of this part. Unplug your Beogram before installation. Ensure that the supply is bolted firmly to the adapter plate, and that the fuse box cover is in place before powering the unit up after installation.
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This shows the original setup:

The first step is unbolting the transformer and the (fake) voltage selector/fuse box housing. This shows the four bolts that need to be removed:
After removing them
the transformer and fuse box assemblies can be 'flipped' out of the enclosure:
The next step is disconnecting the transformer from the fuse box assembly and the rectifier. This shows the fuse box after removal of the fake voltage selector dial:
The grey wires come in from the power plug and the red/yellow wires go to the transformer primary windings:
I unsoldered the red and yellow wires and pulled them out of the fuse box assembly:
Be careful when you try this at home to not melt the plastic fuse box housing with the soldering iron. The next step was unsoldering the wiring from the rectifier (mounted beneath the floating chassis leaf spring next to the transformer):
This shows the unsoldered wires:
and the extracted transformer:
Now it was time to bolt the 3D printed adapter plate to the enclosure. It uses the same bolt holes that were used to hold the transformer in place:
This shows the adapter bolted in:
The next step is soldering the provided wire jumper to the fuse terminals previously connected to the red/yellow wires towards the transformer. This shows the wire jumper inserted from the bottom into the fuse housing:
And on the top side soldered to the fuse terminals. Left
and right:
It is a good idea to leave the fuses in place while doing the soldering. It will keep the fuse terminals in the proper orientation while they get hot.
Once the wires are soldered in, they need to be fed out of the fuse assembly through the 'exit channel' along with the grey power input cable:
Then the fake voltage selector can be stuck back onto the assembly,
which then can be bolted back to the enclosure:
This shows the fuse holder assembly back in place:
The next step is soldering the leads to the in- and outputs of the TPP30 supply's breakout board. First come the leads to the fuses housing assembly. They solder to the terminals "Input 100-240V AC~". Polarity does not matter since these wires carry AC:
Then the red and black wires originally connected to the rectifier output are soldered to the terminals labeled "Output 26.5V DC=". Make sure the red wire is soldered to the "+" labeled terminal and the black to the "-" labeled one:
Now the TPP30 assembly can be turned around and bolted to the adapter with the three provided screws:
Make sure that the in- and output wires are properly fitted into the cutouts on the adapter.
The final step is replacing the original fuses with the new 1.6A fuses provided with the TPP supply. It is easy to remove the original fuses by pushing them out with a suitable screwdriver:
 The new fuses provided with the kit can easily be pushed into the holders with a finger:
The final step is replacing the fuses cover. If it is not in place there will be potentially lethal voltages on the fuse terminals once the Beogram is plugged in. This shows the completed setup in place:
I plugged the Beogram in for a function test, and everything worked very nicely! Absolutely no noise from the supply! Beolovely!

Next I measured how much current the supply draws under the various operational modes of the Beogram.  As expected, the maximum current was drawn under 'play condition', i.e. platter motor running, solenoid engaged and the carriage moving towards the center of the platter. This shows the measurement:

The multimeter is connected between the fuse terminals on one side and set to its 10A range. In this setting it essentially acts as a small current sensing resistor in-between the fuse terminals, and the voltage drop across this resistor is converted into a proportional current reading.
The display shows 0.2 Amps RMS. This corresponds to about 24W power at 120V. In other words, the supply runs at about 80% of its maximum capacity of 30W. 80% is the usual engineering safe margin for reliable long term operation. All good in the power supply department! I should point out again that this new power supply only works in tandem with the Efficient 22.8V Power Supply and Main Capacitors for Beogram 4002 (Types 550x), which significantly reduces the power intake of the Beogram compared to the original setup. Therefore, please do not use the TPP30 supply if your Beogram runs from its original linear voltage regulator based 22.8V rail. It would not be safe and the fairly expensive TPP30 might suffer premature retirement...;-)






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