I recently received the PCBs, the DC platter motor and the RPM panel from a
Beogram 4004 for restoration. As usual I started with the platter motor since it
can take a few days until the oil infusion of the bearings is complete. This
shows the motor as received:
![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEgZeInF-XY5FWvZLPYytYHsnMAGuAJeONXQCt3aA18Y7DBUC9s6IAYC0ss5b4JK-nRTVFJSeJfPbUlWttBNtMxr9ps9jnEEsOAx4Q0uG2N985UVOH1BrjuGiEs1gQ-sOT54-uxBdRLGXQxh7F8ZsoVeiy2bZEUHK9i9ck8fRoi6WPkNehJvp6EFRVuLM1w/s600/1.jpg)
I disassembled the motor to extract the bearings:
![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEirCPwxf9QQyaB99tdGzH3tMAZu_UTwhGRYOO6xP249FTxJ6NpBUPSasb7pPtrbSkDQREPowa_tbFlwE8hVjAwc_AGxRjsyi8U1iESw1efrEr24OjFJgzbuTwESUTBra5mKtDpe1yRoDACHTyRY3yTOyNbMXA4h05WBqSJja94sf2mbR37sK8XMHOuNlTA/s600/2.jpg)
The bearings are the two small donuts on the black pad upfront. I immersed them into synthetic oil and pulled a vacuum. Immediately strong bubbling started:
![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEj0em0hH7esP8KFKatFAwHpSMEKXaprp2Wh7yCHAtqcu2NNXoWW_S6-Cso_xOfLLiZBluArO0wNPYVzncgmsmfz3SxJrn7WdxayRATpysTIqRjWyx4rOP9aA4m8_Qw5VZytOMfJcoing4N7-OQ2ozOQ2nPSTkB0DnduJVeDQd0nzHxuhrMsW6lNHQdIWrY/s600/3.jpg)
This bubbling represents air that is drawn from the empty pores of the Oilite bearing material, making room for oil to diffuse into the material.
While this process was going on, I focused on the other tasks of this project. First I restored the main PCB. This shows it in its original condition:
Here a close up shot of the RPM section consisting of a National brand RPM relay and the two RPM trimmers to its left:
![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEi-z4mfYggmo3Z7OsLnEBcEQ-F1Rci3Pexl9H12uUsQ_X6xIRDWYsaa4AF8Wcf4Is6wjTNcojiql6R5x87N50M-ZR46nHDYqU_NHRTU2jBv1JYGHADYG88O7YvB6tGOR7FKW3hq2iklIGpPPyiKGWOwio_Wn5UucBSFoaHgF5NbuC-kS0RlpWzs0sM808I/s600/5.jpg)
I replaced all electrolytic capacitors, power transistors of the H-bridge and platter motor control and the RPM relay and trimmers:
![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEiuEUaWY-JZcgSKc0D0D3DYMYJR4xSTzHut-8BbACn72zPwYc9Pbf1YAEqD0ePNws2rnSRm6hA_K_WIGo-AGCodQe2shZGJESdc0lTGKhkifyDIo06TkC7OPMpg2zzIJOCAlrgYt8XIAaU1oCJ2Y6vk-DPBBITdF2Ae89iFxjCyarV21qvQ218bUjbGrts/s600/7.jpg)
Next came the output PCB:
![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEhImbPsnzP2ZpbMks2DfTMFiGCO2L2sqFOsOkfNgdFHIgFmcUq5EYdeSWOaea9rJygr9Z2O3PKLvo5vUlaF0n76bImbzAdFCzp5jokfxTSNbz0qVVszqQ40c5T0WtF3uWyEftvEOLYyW1UPbFnCs95ROTNXKIaklmpy7xX-bjJxBi5KKIVrpEauzFGtFfw/s600/8.jpg)
In the Beogram 4004 this PCB carries both the output relay delay circuit as well as the remote control circuitry that allows a Beomaster 2400 controlling start and stop of the Beogram via its remote control.
This shows the output relay circuit:
![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEgf6_IPpWZKdC_WR23AfeLjA1xVOJ_2n1d5pCYRrsnHNCV1PCFh8uKIaRJwzeKQR6BC1t3L6cbbfc9BtwmbdxUUVgg48Rl5yR0IDVm3NgoEFuuGIlHpBqAC5nJy4j5pYBCafDy09PJLqN4sB-wJCrSMpBHr7Yxs2PPKF0JPF5WM99P9D1ZH3WKRIOag61Y/s600/9.jpg)
I replaced all the electrolytic capacitors and the output relay:
![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEjoMqGmy5ECpxybIssvu6LFklhanJM3XUwdu18rvbhhHRGtSeJfV5SLhMQtN2QSNwGEhx9xop84BQqfTeRQfE94MgtEU90t4_Pdi_zEyrWBGYAEulIVwzOP5GHus6K_Ryry49QNIHhi8jn1xzEO5MjiM7fXaGfwODmz4BjiTmp2dNxV1FJhrchYRwOh9sU/s600/10.jpg)
Here a detail shot of the output relay:
![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEhj2xH2eaeM0C43VDmg_Y3Avl24X6zn8hzki6i0zhXd0eIDQwrLPiCz3JMGCWK8eV4ggf6xWE4FpqspOAulRcAMuJ2Zdbj-FM0yMTRleTtyj-4VXRZI9CCuQxcHuef_Z3f3PO0VpkLNfXw2K6bUataaDy62qKOT0BdquJWZCg9xBlr3M9531XtkKE3W04A/s600/11.jpg)
I also installed a (red) switch that allows connecting system and signal grounds in case there is a hum in the output signal.
Finally, I updated the RPM panel with LEDs. This shows the panel on its back which reveals the two bulb covers:
![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEgbfZRvSp9kFvGm5PBW0vfStZFLj0LBX583evbz0JQYoYvpNg9P_dLcmlDu5ADPQlGdjUmjGGocB-TU_5buXWmbCZWaEqkaD0O884-2DyGJT4W53wyqFb0iWPXaJp2uCWGPzrrzOWPh0CUodgQ9-17LYXV-_0dKEBs0bGsLitIjfHiwIVSTgAEfltMpUWo/s600/12.jpg)
I removed the covers
![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEh2tZ1o28-sTO8XVbD8TF6LGpYltVKbO1fzx5Uqj4udJcA6Av3HO5M3jnpud5uSEe8kErN9kJxq7BEdQ5KLIkKbtilSV53wnx6no-i7NRiOUmsP12Ke02WORg4x0jNhSjGXanGkERgRepI-2nbNSo-TCUUUGeF8Oj5HUnlb_2ebe5wrUsFbYrrU25f9vAE/s600/14.jpg)
These little PCBs solder directly to the terminals where the original bulbs connected. They essentially become extensions of the original PCB:
![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEi4WPZB0OhA32I3wNUVgXBR5KFqHlaUGeYo6nKt_4UABI4jYx5rqpmgc35zhp0kfxQnNUga9EgBz37EpRl898upf0RicFoC0fXiMoBYy6egz848d83YjzUmon8yMjv_5ZbFv6Qs4iakurqxL9cvh99EbqBXZ3sTK-oX7hxKlg5gILO182zI2zRe4ZcQ28M/s600/15.jpg)
The boards do not interfere with the bulb covers, which can be installed like before:
![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEgnLGpmLFd1x-Gtj9PEua_lcAkvq-8d44b6X_vRbPKIf384bL6O7gxk-RAomSwpY0JxNMASa6ls1-0AxN53yKEWQKM_ndPxpX4fhKkpbuadKNKKpIsMH3m5WvG6KuKXanoBK1s3CchJtKB0XKsNEoBDLED3GQ5C5Ogpc_HWZI5jKDk3FQCioD-QdUkQfb8/s600/16.jpg)
Now it was time to implant all the components into my bench Beogram. After bolting in the main PCB I replaced the two power Darlingtons mounted on the solder side of this board. It is best to replace these while the board is bolted in. This makes positioning a snap. This shows the original IC1, a TIP120, which is responsible for regulating the 21V rail:
![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEgzZocjMiKuNcYFNIg-8IwUwcI0iQpxiMP9I9UI8GKPvQpPTpPzXTY9ZTRngjwqMFfg-rohiI213rW_HeLKRjswxaKjf3FLi6NyU5n8Bveqps0tT6xGYFYYX1bRDVKM6dnFmXws7SfWUO1KkkD77V4Ozd02dtt_dqjrTWXj4mjqq_FoOdGfMaGEaUiTIoQ/s600/17.jpg)
I usually replace these ICs with stronger types. In this case a TIP102 is the perfect replacement:
![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEgNruGyCRq1_eWue6iPuHMD5WDoRhqEM71D5xu3rEf_QQAbg0AxCuDPupxBwRRdEHxWZvm5-oxbV32s9U1d_pC5rsAd04KpACr_eD2c_9_OmTd-W3r9tnJz6nA9W-NLkNBHqQLJsSb32UU3rVuOFN80qtOH7AvFJYEssHpBKzFwnBRxKRi6Vjf-XRdSrMk/s600/18.jpg)
In this circuit configuration the modern TIP packages need a 100nF capacitor soldered between the Emitter (output) and ground. This quenches a high-frequency oscillation that can occur after the replacement. I also replaced IC4, the solenoid transistor, with a TIP107 Darlington:
![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEiXcpYALRfwbzqttsi5_T0wU-gUnIxjLLCrxl1Apo52jyfMknmJ9Qrxf0uisLfOoeylQOIS2LHYhwTKOAxTTIQtWbnkfTmG1zUvNCKxruEdfloXlb0qLsOuVLzCqDOm97k9fg4YLDyFphdrEdblKf_-1otbe3RwrtHSUT9v8vSZVL42Sggp75-xYLBSVMs/s600/19.jpg)
The oil infusion of the motor bearings had come to an end and I extracted them from the vacuum chamber:
![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEiTYTicY7TmUA4AJkeP4l0-3yvL3NYa3VSirA6QwIgjznSJss52FCg70v55hpozrY8_ehz-sVy0ss4Rwa0xUP0u8Ch3FczWPSdwyVYrcFenY1MVjAzlisSJ35uQDzbio5q-9gAzvCzhCdggsLZselGhuE_FVAIuK9NPShKDxEK8HUtoUfOfJZ-gFlxUk-U/s600/20.jpg)
I reassembled the motor and implanted it along with the PCBs and RPM panel in my bench unit. Then it was time for a RPM stability test with these components. This shows the
BeoloverRPM device in action:
![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEh3wRPKq-kXAkjcbKjLPgQrMND5K4alhxKK0Ij3IgG53hFS4_3nPG8IR3GMcRbbTkpayP0ED21edvSZG2NUWlPhPUEwP-Lg4N7jOrn8wKAHVdnFg56bghvApb7i2l0wSG69UEU8eF_dXKgd555zEqBCxISHfjcpSSdnYuFzrctiSDLgjtTjCwVuyQvGXI0/s600/21.jpg)
In its 'slow' mode it outputs the RPM in 10s intervals. Using a terminal program on a PC or Mac the RPM can be logged for extended periods of time for generation of a RPM stability plot. This shows the 24 hrs RPM stability graph I measured for this motor:
It is slightly choppy. This is a result of this motor having been opened before without noting the original orientation of the top bearing. If the bearing is not installed in the same orientation there may be a period where the shaft polishes a new segment of the bearing as it is pulled towards the platter by the belt. In my experience these small variations slowly go away after playing the deck for a while. At any rate these fluctuations are much smaller (~0.3%) than what humans can typically discern when listening to music (>0.7%). So this motor is ready for duty again!
I also measured 'wow and flutter' (the short term RPM fluctuations introduced by the feedback speed control system) using the 'fast' mode of the BeoloverRPM device. In the fast mode it logs the RPM after every passing of a platter rib. This reveals a pattern that repeats every 24 measurements, i.e. after each turn of the platter. It is a result of minute spacing variations between the ribs due to manufacturing tolerances. The wow and flutter RPM changes are superimposed to this pattern as a sine-wave like feature, which is normal for analog feedback-based control systems:
Evaluation of this pattern yields a wow and flutter number that is smaller than 0.1%. This is slightly larger than what the manual specifies (<0.05%), but this may well be a result of the different way they measured wow and flutter in the 1970s, where they used a test record and an analog filter based 'frequency analyzer'. The joys of analog audio!...;-).
In summary, this was a successful restoration project and these components are ready for duty again!